Aye aye maties!
Well, what an update I have for you...
I finally got sick of the bike sitting in the garage not running. Other more important work-related projects came up, so I wasn't going to look at it anytime soon. Took it to the shop, just wanted to have it running!
Well it turns out I really buggered up when I put the head back on, there was an o-ring missing, apparently! WTF?? I cannot believe I would do that, but anyway... they also said the base gasket was on upside down but that shouldn't have caused any problems. There was coolant in the cylinder, which wouldn't help.
They cleaned that up and also looked at the flywheel, woodruff keys etc. All good no problems with the engine. They cleaned some dirty connections and got a good strong spark.
The problem is - the engine has some crazy compression. I should get them to measure it, they did have it running & idling, but didn't ride it. They had to get the biggest guy in the shop to kick it, and he did it so much that it warmed up the engine just from that! Then they still had to use AeroStart to get it started.
Next day, cold start - not a chance.
So it looks like I just need to get the head modded again to reduce compression??
The head was modded down to 1.3mm squish (as mentioned previously in this thread), but just the squish, no chamber reshaping etc. Would that a make a difference? I'm going to get it out of the shop now anyway, already racked up a workshop bill of $847...
I am thinking I will just take the head to the local engineering shop and get them to reshape the combustion chamber and machine the squish out to a larger measurement - but not sure what? 1.8mm? 2mm? Or do you think it could be some other problem that they're not thinking of, I didn't think that the head mod would affect it so adversely? Awaiting your knowledgeable responses!
